Jump to content

51 B3B build thread - after all these years


bkahler

Recommended Posts

On 5/16/2022 at 10:44 PM, JBNeal said:

would a 3M trim adhesive be less prone to cracking than JB Weld?

 

"Adhesive is made to create permanent adhesion between dissimilar and non-porous materials such as plastic and fully cured painted automotive surfaces"

It doesn't really seem to be suitable for metal to metal applications.  I've never used the stuff so I don't know how hard it gets.  

 

18 hours ago, Brent B3B said:

Lol Man, I figured you would have been more supportive of a “JB” product ?

 

Gotta admit, that was a good one ?

 

3 hours ago, ggdad1951 said:

it's light tack welds, you might just get away with that and over coating with some paint....just sayin.

 

maybe find someone with a TIG to fuse on the bracket bit?

 

After reading Mark's reply and looking closer at what needs to be done welding will likely be the answer.  I have a TIG welder although I am nowhere near proficient at it.  I also think wrapping it in wet rags and using the MIG welder to do quick spot welds might do the trick.  Worst case is I can have the painter touch up any spot that I damage with heat.

 

I'll  ponder on the situation for a day or two and let y'all know what I end up doing.

 

 

 

Link to comment
Share on other sites

Just now, bkahler said:

After reading Mark's reply and looking closer at what needs to be done welding will likely be the answer. 

I think tig welding would probably be the best choice, even if you need to practice on some scrap metal.

You could use it as a learning opportunity  :)

 

Although your original idea may work fine as well.

While I like JB weld, it has a place to be used .... I have some that I opened & used a small portion.

Later I needed to use it again, the cap was stuck on & only way to use it again is to cut the top off.

 

Next time I wanted some I bought this product instead, pretty comparable in price. Twice the amount of product.

It comes in a layered roll. Just slice off the amount you want, knead it together thoroughly .... I assume if stored properly  it will be fine to use again the next time is needed. You can grind, sand, paint it just like JB weld.

 

71+ByCnGN5L._AC_SL1500_.jpg

Link to comment
Share on other sites

2 hours ago, Los_Control said:

I think tig welding would probably be the best choice, even if you need to practice on some scrap metal.

You could use it as a learning opportunity  :)

 

Although your original idea may work fine as well.

While I like JB weld, it has a place to be used .... I have some that I opened & used a small portion.

Later I needed to use it again, the cap was stuck on & only way to use it again is to cut the top off.

 

Next time I wanted some I bought this product instead, pretty comparable in price. Twice the amount of product.

It comes in a layered roll. Just slice off the amount you want, knead it together thoroughly .... I assume if stored properly  it will be fine to use again the next time is needed. You can grind, sand, paint it just like JB weld.

 

71+ByCnGN5L._AC_SL1500_.jpg

 

Practice?  Who has time to practice?!!  :)

 

That's an interesting looking product.  I'll have to keep it in mind for future projects.

 

I talked to the painter and he suggested welding as well and would fix any damage I might cause to the currently finished product.

 

 

  • Haha 1
Link to comment
Share on other sites

Put the seat back cushion in last night so I could measure for lap belts.

 

I forgot just how comfortable the seat actually was to sit in.  Much better than I remember.  Interestingly I found the truck seems taller than I thought it was to climb into.  I took a measurement and found from the ground to the very top edge of the bottom cushion was 43".   That's more than I expected.

 

20220517_160034.jpg.49c6f02d3b28bdebd76e6dfc387040c5.jpg

 

20220517_160018.jpg.79a128fe48e694f3c9cc009c74ea10b7.jpg

  • Like 1
Link to comment
Share on other sites

What's that old adage, fix one leak and two more show up?  Well that's what just happened on the fuel system today.  I replaced the tube going from the front carburetor to the rear to due to the mucked up fitting.  That leak is now gone.  One of the two new leaks that are now present is where the top housing of the carburetor bolts to the carb body.  Back when I rebuilt the carburetors I spent a lot of time getting the two mating surfaces flat using a thick piece of glass and sand paper.   I'm actually surprised that it's leaking there.  I'll have to pull the cover off to see what I might have done wrong.  I'm wondering if that could that be a symptom of a leaking float needle?

 

I believe the second leak is actually the result of a cheap porous filter housing casting.  The leak seams to be coming out of the top of the casting and not at any seams or joints.  I bought it new and I'm sure it's a cheap Chinese knockoff which means I get what I pay for :(

 

I also started filling the coolant system today so tomorrow we'll know if that problem is fixed.

 

Assuming I can get the fuel system leaks fixed and the coolant system doesn't leak the engine is 100% ready to try and start.  All I need to do at that point is turn the key and stomp the starter :)

 

20220518_173345x.jpg.96f5213f0f40641cea2e6dbb1a5d7e56.jpg

Edited by bkahler
Link to comment
Share on other sites

It would appear I'm going nowhere fast :)

 

While poking around looking for more leaks I noticed this one on the top front of the radiator.  It appears to be leaking right at the seam.  I guess the next step would be to pull the radiator and take it back to the shop to be fixed.

 

20220519_161423x.jpg.0d7ccdf3f46898e2abad08207fb287df.jpg

 

I'm not sure yet but I think I might have missed putting sealant on the threads of the bolt holding the generator pivot bracket to the water pump.  I'm not 100% convinced it's not residue from previous leaks from above so I'm going to watch it for a little while to see if it progresses.

 

20220519_161745x.jpg.39f05333a1af947369b39542a5717384.jpg

 

 

As far as the fuel system leaks I'm beginning to think there is nothing wrong with the front carburetor gasket.  I pulled the top housing off of the carburetor and the bowl wasn't filled entirely which tells me fuel hadn't reached the level where it would be forced through the gasket.  The other reason I think that might be the case is because the top surface of the carburetor housing was damp and it wouldn't have gotten that way from fuel seeping past the gasket.  

 

I think what happened is a mist or very faint stream of fuel is/was coming off the top of the fuel filter housing.  You can see in the picture below that the top of the filter housing is wet but there is no fuel around the fittings or around the edges of the filter.  It's coming through the top!

 

20220519_161051x.jpg.1620a8485782c20d9a34ce2629106626.jpg

 

I'm not going to pull the radiator until I'm sure I've spotted and fixed all of the other coolant system leaks.  Once I'm convinced there aren't any more leaks then the radiator can be fixed.

 

What fun :)

 

Link to comment
Share on other sites

Well the news just keeps getting better and better.....

 

The radiator shop that has done all of my radiator work for years is out of business :(

 

Aside from this one small leak they always did great work.  So now I have to try and find a shop somewhere in the region that can fix it.  

 

While checking for leaks yesterday I found one between the head and the water pump just on top of the block.  I wiped it clean thinking it might have been from when I replaced the thermostat housing.  Fresh coolant showed up overnight so that tells me either the head gasket is leaking or the the back side of the water pump is leaking.  I'm going to have to keep wiping it down until I find find out from which direction it's coming from.

 

I've built and installed a lot of engines and have never had this many issues with small leaks before.  Starting to get frustrating!

 

20220520_102613x.jpg.6020f1e5d100a9d5db363ce8fdeda536.jpg

Link to comment
Share on other sites

Well, I think it's pretty conclusive that the gasket between the water pump and the block is weeping.  So it's time to drain the coolant system again and then pull the radiator and the water pump.  

 

So far the closest radiator shop I've found is about 2 hours away :(

 

20220520_162914x.jpg.2e5978b18d8b7ef082dc9717514945de.jpg

Link to comment
Share on other sites

I have ordered gaskets and hose clamps from DCM Classics and I should have them early next week.  After doing some research I've decided to try and solder the radiator seam myself.  From what I found, using a micro torch with solder will allow me to target the small spot that is leaking.  Solder and acid flux is on order as well and I'm hoping to work on the radiator next weekend.

 

This morning I tackled the damaged driver door catch.  Whoever made the "repair" was more of a butcher than a repairman.

 

They brazed a small bracket on the inside of the door that the door catch arm passed through.  It definitely worked as a door stop but it was crude at beset.

 

20220522_095405x.jpg.1d9e5d0c6a49a4f4acb6bf612ee736b0.jpg

 

20220522_095422x.jpg.d7d3ec7b887ea6d4e379b30911af71a6.jpg

 

From the looks of it he used a large round punch from inside the door and beat the opening until it was bulging towards the outside edge of the door.  

 

20220522_095903x.jpg.a669c6391fbe5307038192af7ba52dc0.jpg

 

 

After removing the brazed in bracket I did what I could to beat things inward and used a small rotary grinder to cut out the old broken pieces.

 

20220522_104005x.jpg.0c2f1aa888d3ea6217a7a958229e5bcf.jpg

 

 

if you look close enough you can see where I've sort of reversed the direction of the bent opening.  This will allow me to get the new catch piece inside the opening in the right orientation to work with the door catch arm.  What I need to do now is figure out a way to flatten the opening.  This will likely require some heat, a bucking bar and some help.

 

20220522_104112x.jpg.8db768ba24d4f974a345fb3eb26c8c79.jpg

 

The goal is to use the pieces in the picture below to repair the opening.  The metal plate will be on the inside of the door and the catch piece will be between the outer skin and inner support frame where it belongs.  I plan on using a couple #10 screws to hold the two pieces together, sandwiching the inner door brace and once everything position I'll weld the plate in place from inside the door.  

 

20220522_150216x.jpg.87f713580c4f61ff9ac875057b62a62d.jpg 

 

Stay tuned...... :)

 

Edited by bkahler
Link to comment
Share on other sites

6 minutes ago, LazyK said:

where did you purchase your door catch or is it something you fabricated?

 

JB found them at LMC Trucks.  The hole spacing is slightly further apart, 1-3/8" vs 1-3/16" but as mucked up as mine was that turned out to not be a problem.

 

 

Link to comment
Share on other sites

8 hours ago, JBNeal said:

ya might be able to flatten that opening area with a bolt-flat washers-nut clamp:  washers on both sides of opening, tighten nut down, smack it with a hammer and call it good.

 

That's definitely an idea worth trying however I have a hunch that I won't be able to get a big enough washer through the rectangular opening on the outside.  I'm pretty sure the opening is only 7/8" wide.  However after thinking about it for a few minutes a rectangular flat plate might substitute for a washer and I believe a long narrow (7/8" wide) strip with a hole drilled in it just might work :)

 

I'll report back this week.

 

Thanks!

Link to comment
Share on other sites

Well for what it's worth the door catch repair is done.  From the inside it's not very pretty but I think it's serviceable.   I debated for a few minutes as to whether or not to weld the plate in place but in the end I decided it would be stronger and make it easier to replace the catch if it ever breaks again.

 

20220527_130958x.jpg.c21166030f6b06f0063774c76eab6915.jpg

 

20220527_132155x.jpg.b08c8090c7f60de0157cc2829dae9880.jpg

 

 

For the most part I think it's a good repair and should work just fine.  The outside opening needs to be smoothed out some and I'll have the painter take care of that little problem.  The door is heading to the painter this afternoon.

 

20220527_130909x.jpg.181ee14d79200c1fc739d9d52dc8a66a.jpg

 

20220527_130924x.jpg.302b0f63d636713cc1e0555756a359cb.jpg

 

Big thanks to JB for finding a source for the door catch parts, it's kind of hard to repair something if you don't have parts :)

 

I now have all the parts and supplies on hand to repair the radiator and the water pump gasket.  I hope to have that work completed by the end of the Memorial day weekend.

 

 

  • Like 2
Link to comment
Share on other sites

I was kind of surprised to find after reading the manual page that Merle provided that there is no adjustment on the fuel gauge. 

 

I had 5 gallons of gas in the tank and the gauge needle hadn't moved so I assumed that either the gauge was bad or the new sender was bad.  First thing I did was disconnect the wire between the gauge and the sending unit.  Next was to test the sending unit.  I believe the sending unit is a 90 to 10 with 90 being empty and 10 being full.  The reading with 5 gallons was 70 to 71 ohms.  I poured about 1/2 gallon more into the tank and the reading changed to 69 ohms.  That told me the sending unit was working (it's new so it should be good!).

 

Next I grounded the sending unit wire to the gauge and the needle pegged at full!  Ok, the gauge is good, or at least functioning.  I then hooked a 0 to 100 ohm wire wound potentiometer between the gauge and ground and slowly started turning the pot until the needle moved on the gauge.  At 63 ohms the needle was just starting to come off Empty.  

 

I plan on pouring more gas into the tank In order to determine just how much gas will be in the tank once the needle drops to Empty.

 

The only thing I won't know is how much gas is in the tank before you can no longer suck anymore out.  

Edited by bkahler
Link to comment
Share on other sites

1 hour ago, bkahler said:

The only thing I won't know is how much gas is in the tank before you can no longer suck anymore out.  

 

i'm sure they all vary a bit.  with mine, when the needle hits empty, i am out of gas in about a mile, but the truck only gets around 5 mpg.  when i do run out, i can put about 16.5 gallons into it, so there's about 1.5 gallons that can't be used.

Edited by wallytoo
Link to comment
Share on other sites

On 5/28/2022 at 5:16 PM, wallytoo said:

 

i'm sure they all vary a bit.  with mine, when the needle hits empty, i am out of gas in about a mile, but the truck only gets around 5 mpg.  when i do run out, i can put about 16.5 gallons into it, so there's about 1.5 gallons that can't be used.

 

A 1.5 gallon heel in the tank isn't to bad.  I'm hoping my 1/2 ton gets a little more than your 1.5 ton truck :)

 

 

 

 

Edited by bkahler
Link to comment
Share on other sites

23 minutes ago, wallytoo said:

 

the b3c that i drove in high school got about 15 to 17 mpg.  three speed fluid drive.

 

That would be a lot better than I was expecting  I was thinking 9 to maybe 12.  I do have the 3.73 diff so that's in my favor.

 

Link to comment
Share on other sites

i don’t know how your dual carb setup will influence your mileage, so you could be right as far as a bit closer to 12 mpg.  my b3c has its original engine and single carb, but hasn’t been out of my dad’s garage since 1988.

Edited by wallytoo
Link to comment
Share on other sites

Maybe some super glue for the glass cracks?

 

?

 

DJ

  • Haha 1
Link to comment
Share on other sites

Join the conversation

You can post now and register later. If you have an account, sign in now to post with your account.

Guest
Reply to this topic...

×   Pasted as rich text.   Paste as plain text instead

  Only 75 emoji are allowed.

×   Your link has been automatically embedded.   Display as a link instead

×   Your previous content has been restored.   Clear editor

×   You cannot paste images directly. Upload or insert images from URL.

×
×
  • Create New...

Important Information

We have placed cookies on your device to help make this website better. You can adjust your cookie settings, otherwise we'll assume you're okay to continue.

Terms of Use