Jump to content

JBNeal

Members
  • Posts

    7,221
  • Joined

  • Last visited

  • Days Won

    82

Everything posted by JBNeal

  1. VINTAGEPIC: saw this Route Van on the FB
  2. I do not see a casting date on the head, so I am not sure what is going on there. My interpretation is that flathead block was cast November 20, 1950, first hour day shift. The crankshaft p/n appears to be 952068; according to my B-series truck parts manual, the crankshaft for the truck engines was 952066...maybe your crankshaft was from a car engine? The stamped serial number on the block could give a clue as to what is going on with the engine with some deciphering
  3. would ya care to elaborate, preferably with side-by-side comparison, as to correctness...?
  4. Have ya tried SD Spring?
  5. have ya tried a gasket sealant?
  6. on one adventurous summer Saturday night several years ago, I took the '48 onto I-35 for a 2-mile stretch, got the speedo up to 70 (don't know how accurate that was), and that ol' truck was vibrating through the floorboards something fierce (as most of the original cardboard interior insulation is gone)...it seems more comfortable around 50, especially when stomping on the brakes (FYI that's a stock 230 3spd w/ 4.10 rear)
  7. I tried this, then heard about this, so now I do this
  8. the second spring argument again... according to the parts manual, there is a spring on the bell crank (14-14-1: 640 407) and a spring for the throttle return (14-06-1: 1088 169) that is routed to the floorboard...the assumption is that THIS is the original setup. I am assuming that the second spring was added as needed as part of some sort of service bulletin to address wear along the throttle linkage...after all, it is only a gdspring
  9. I had planned on doing the rework on The Money Pit in a manner similar to what you are doing here: remove front sheet metal & engine; send engine block to machine shop for rework; disassemble the bed and stack the panels outdoors to be finished last; cleanup & repair rear axle & suspension; tilt cab back to the rear of the frame to cleanup cab bottom (maybe with roll-on bedliner) and frame section; cleanup front frame & suspension; test rebuilt engine & transmission before installation; etc. etc. etc....this approach takes up less shop space and allows for parallel work to be done as weather allows. Powertrain work, sheet metal work and initial paint can be done in a smaller indoor space, the frame can be cleaned up outdoors as it does not have to be perfect (who's gonna see it when it's all put together?). The 500 gallon LPG tank that I reworked 4 yrs ago outdoors still looks as good as it did when I finished, so that has been my test case that has proven that this method works as long as things are kept clean. Painting was done with a foam roller, and the entire project cost less than $50. Final paint for the entire truck can be done in an adequately sized indoor space, taking up much less time inside the shop space, allowing other projects to occupy the shop as needed
  10. additional information - Man in the High Tower
  11. I have been swapping stories with Dave over the years before & after he dropped off of this forum. He sent me his notes on roller paint jobs, and we went back & forth on the specifics when I was refinishing my 500 gallon LPG tank a few summers ago...I had to scale back that job cuz at the halfway point, his methods were yielding such good results that the shine off of that tank in the summer sun was becoming a blinding nuisance to passersby, something he found amusing. I had not heard from him in a few months and began to wonder if he had moved on as he mentioned something about not getting any younger...his passing saddens me and he will be missed
  12. contact cement is used in fully adhered rubber roof systems
  13. the original wiring diagram shows voltage connected to the horn, with the horn button acting as the ground contact switch and no relay involved. If you follow the path to ground from the horn button, continuity has to pass through at least one bearing, the steering gearbox case, the frame, and several bolt connections before getting to the transmission case where the battery was originally grounded. Over time, corrosion can increase the impedance at these locations, decreasing horn effectiveness, especially in the original 6V setup. I put together a modified wiring diagram that shows a separate ground wire that would have to be installed to a modified horn button that could bypass all of those connections with a clear path to ground. At some point I may get back to finalizing this horn button modification, but until then it's just pie in the sky
  14. the larger openings would allow for more flow which can boost filtration rate and heat transfer...I think the gauge pressure would drop slightly at low RPMs but the increased flow would offset this; pressure at higher RPMs I believe would still be regulated as with the original pump
  15. Updated Build Record Information Request
  16. US War Dept Build Card info
  17. I have several of that horn on the left, but I don't know for sure where they came from (cain't get any of them to work either)...the horn on the right looks similar to the B-series horn, which can be had in a dual horn setup
  18. The dual horns I snagged are similar to the set posted, but this one popped up on eBay back in '09 and it looks similar to a set I saw in a Bunn book
  19. B-1 vacuum wiper arm on the left (sorta) ===>> <<=== B-1 electric wiper arm on the right additional information - electric and vacuum wiper motor comparison
  20. additional information - Chrysler "Coming Home" Commercial
  21. JBNeal

    PAINT!

    paint it any color ya want, a slammed S-10 is a rolling speed bump
  22. additional information - bullseye halogen conversion
  23. maybe they sweated some old lead wheel weights in there prior to paint
  24. The B&B carbs were plentiful on the 1/2 tons with the 218, as the Strombergs were standard on the 1-tons with the 230. The Stromberg setup has the fuel filter bowl that is outboard of the manifold heating, where as the B&B setup has the fuel filter bowl over the manifold heating. My '48 1/2 ton has a 230 in it with the B&B, and it seems to have better throttle response than the Stromberg in my '49 1-ton with its 230. I'm almost certain this is due to the vacuum advance in the 1/2 ton distributor; the 1-ton distributor only has a mechanical advance. My experience is that the B&B is more prone to fouling than the Stromberg...this has manifested each time I've had the trucks sit for an extended period, as the Stromberg seems to free up immediately whereas the B&B sputters for awhile before the fresh gas cleans out the passages. So either works as long as they are fairly clean & set properly
×
×
  • Create New...

Important Information

We have placed cookies on your device to help make this website better. You can adjust your cookie settings, otherwise we'll assume you're okay to continue.

Terms of Use