Thanks! I started off by cleaning out the back of the gauge, then tested it with air. It was right on the money. Reassembled it and ran the motor and the pressure looks good now. It's actually showing slightly higher pressure than before across the board.
I think the relief valve was stuck in place, it took a bit of wiggling and turning it inside the get it out. Cleaned up that assembly and replaced it was as well (without the nut). Always pleased when the simple solution in the correct one. I'll sure be watching the pressure closely as I continue to wake the truck up.